Analisis Kinerja Coal Mill Unit 4 PT. PLN Indonesia Power UBP Pangkalan Susu

Authors

  • Moch Fikar Surahman Program Studi Teknik Mesin Fakultas Teknologi Industri Institut Teknologi Nasional Bandung Author

DOI:

https://doi.org/10.71417/jpc.v2i1.134

Keywords:

Coal Mill, Efisiensi Energi, HGI, MPS160HP-II, PLTU

Abstract

Coal Mill serves as a critical component in Steam Power Plants (PLTU) for pulverizing coal into fine powder ensuring efficient boiler combustion. This study aims to analyze the performance of Coal Mill Unit 4 at PT. PLN Indonesia Power UBP Pangkalan Susu, type MPS160HP-II. Quantitative descriptive research was conducted through field observation in June 2024. Population comprised 5 Coal Mill units (4 active, 1 standby), with sampling focused on one unit comparing design vs. actual data. Instruments included observation sheets and Central Control Room (CCR) data, analyzed using energy efficiency formula   and production efficiency  . Results revealed production efficiency of 89.5% and energy efficiency of 84.5%, below design standards due to 35% coal moisture, HGI 50, air-coal ratio 2.44, and mechanical wear. Conclusions recommend real-time coal quality monitoring, predictive maintenance, and air ratio optimization to achieve efficiency above 90%.

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References

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Published

2026-01-30

Issue

Section

Articles

How to Cite

Analisis Kinerja Coal Mill Unit 4 PT. PLN Indonesia Power UBP Pangkalan Susu. (2026). Jurnal Pengabdian Cendekia, 2(1), 350-358. https://doi.org/10.71417/jpc.v2i1.134